Sunday, 23 February 2020

Loco Anatomy & Injectors - Mutual Improvement Class

Saturday arrives with two Mutual Improvement Classes in the conference room at Weybourne.

A group of cleaners, drivers and firemen gathered for the day for a general presentation in the morning concentrating on boilers, smoke boxes and fire boxes, followed by a quick overview of other locomotive components.

Boiler from SR West Country Pacific 34010 ‘Sidmouth’

Regulator from BR Standard 4MT 76084
The afternoon session was an in-depth presentation on the main different types of injector; lifting injectors and gravity fed injectors; live steam and exhaust steam injectors.

Injectors from BR Standard 4MT 76084


Turn 18 - Cleaning the WD and the B12

Well it's been a while since I have done a cleaning turn, four months in fact. I had a read of my older blog posts in order to remind myself what to do!

I was rostered as Cleaner today, with Dan rostered Third Man - so there are effectively two of us on cleaning duties. We both signed on just before 06:00 with Fitter Bob, and set about preparing the WD. The B12, which had been rostered all week, had failed with a poor air pump the day before, so the WD was already warm. I took the front end, Dan took the firebox. The smokebox had a barrow load of ash in it; I remembered to brush down the sealing surface around the door for once:


It was just getting light as we got to work:


Smokebox done and the fire under way, I turned my attention to cleaning the paintwork with paraffin & oil. I took care to rope my ladder on:


I worked my way around the loco and tender.


Fireman Paul and Driver Dave turned up to do their bit, and Dan moved on to cleaning the wheels. By the time I had finished, there was enough pressure to get on the pit. While the footplate crew finished oiling up, asking out and blowing down, I busied myself cleaning up the cast brass nameboards a bit. That done, we stood back while Fitter Bob loaded coal into the tender. As we neared departure time, the crew departed to get changed. I stayed on the footplate chatting with Fitter Alan, and kept an eye on the fire.


I must work out what this lever is for. The one on the left is the drivers side injector water valve - I think the other one is the cylinder cocks, though I am not sure what those two catches are for.


My time on the WD was drawing to a close. I had a last look at the fire, added some coal at the front and back corners and waited for the crew to return. I was pleased to see it flaming nicely as I climbed down to go and find another job.

With the WD in service, I turned my attention to the B12, which was going out the next day. The bits and pieces I need were to be found in the cleaners store:


The B12 is cleaned with citrus cleaning fluid and wax polish, which takes a long time if you are to do it properly. The citrus cleaner loosens oily soot nicely, but you have to get it off the paint and onto the cloth which takes three cloths used in sequence and of course these need to be replaced as you get around the loco - probably twelve cleaning cloths will do the whole boiler cladding. You then need two further cloths to apply and buff up the polish. I started at about 09:45; by 12 I had done one side. My excuse is that I had been out with my grandsons the day before which is always pretty tiring! I cleaned the soot off the other side but didn’t get time to polish. By the time i was done Fitter Alex had lit a warming fire for the next day.


When the WD returned just before 11, I made sure to meet it - it was carrying my breakfast!


I ate my bacon & egg roll on the footbridge watching the Class 37 heading off to Holt to pick up a good train:


Just before 13:00, the rain began to fall. Fortunately I had got as far as I was going to go with the B12  and it was time to clear up the Cleaner’s Store and the yard. I filled in the Cleaner’s check sheet to record what I had done and went to get changed.

Next turn is a Third Man turn on a wedding train, next weekend.

Friday, 21 February 2020

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Who knows what this lever does???

Friday, 7 February 2020

Shed Turn - Crossheads, Injectors and Clacks

It’s Friday, it’s February; there are no trains running but we must get a railway fix, so it’s time for a Shed Turn. As a volunteer, I can do whatever hours I like but when I am on the railway I like to put a full day in, so I start and finish with the shed staff.

Today, the early morning sees a departure from the boiler shop - a newly refurbished boiler heading back to join its frames at a railway in Belgium.


Further along the back road, the S&DJR Fowler 7F waits its turn for more attention to the springs. Behind it is the Grafton steam crane, which is waiting collection by it’s new owners - it will head down to Sheringham soon for road transport to, I think, Whitwell.


Today however is going to be centred on the continuing winter maintenance on 76084, the BR Standard 4MT 2-6-0 currently in residence, affectionately know as the Pocket Rocket. It’s part way through a valve & piston overhaul; the valves I cleaned a couple of weeks ago are in the machine shop and the railway are manufacturing some new piston rings, judging by the pile of broken ones I saw laying about.

Walschearts Valve Gear

Today, apprentice Keirhann & I are going to remove the cross heads which are currently tied in place with blue rope. In this shot, we have removed the drop arm and union link, and we’ve positioned a hydraulic table behind the guide bars ready to catch the heavy crosshead when we pull it out. 


And a bit later, we have the two crossheads on the bench, awaiting inspection. I’ve cleaned the drop arms and the union link, still fitted to the one in the foreground.


The next jobs are all about inspecting & refurbishing various valves & other equipment. While nosing about, I noticed that the faulty regulator was still out, noticeable by it’s absence in this view through the dome. Those are mainly fire tubes you can see beneath it; notice the operating rod passing out of the boiler toward the top of the picture an the main saturated steam pipe heading off to the right, towards the smoke box:


Here’s a different loco, with a similar (though not identical) regulator. This is the GCR Stanier 8F, 48305. This still has the regulator operated with a longitudinal shaft from the centre of the back head, rather than the later radial shaft used in the BR Standard locos, but it gives you a good view of the first (or ‘pilot’) valve on top of the second (or ‘main’) valve beneath. These are arranged so that the initial movement of the driver’s lever opens the smaller valve, followed by the larger valve with more lever movement providing better control of the steam flow.


The reason I was on the running board was to help Keirhann replace the steam heat valve, which he had serviced, re-cutting the seat earlier in the week. This was a straightforward job, but some of the bolts were a bit tricky to get in and tight due to the mounting bracket.


Our next job was to remove the two injectors for cleaning, which was to take most of the rest of the day. Here’s one, withdrawn from it’s housing under the fireman’s side of the cab:


Have a look at this diagram:


The parts we have removed are the black sectioned bit in the middle, including the delivery cone, the renewable nozzle and the combining cone with it's flap. Here it is again, after an hour in the descaling bath:


It doesn’t look too bad does it. We needed to strip it further for cleaning, which involved splitting the two halves. In that square block in the middle, on the RH side of the big thread is an anti-rotation pin which prevents the two halves coming undone. We spent about two hours removing two of those pins before we were able to split the two halves and finish cleaning the injectors.


Have another look at the diagram. Here I have my spanner on the delivery clack inspection cap nut:


Here's the clack valve, before cleaning:


And here is the clack valve seat as I found it:


Here it is again, after 15 minutes work with some fine grinding paste. You often get a whiff of steam out of the overflow when the injector is not running, which is a result of the two clacks leaking.


Next we turn our attention to the top clacks. Keirhann & I are now high up on the running boards, and we have strapped ourselves to the hand rails to save any accidents. We are throwing our weight about a bit up here, using flogging spanners and it would be easy for a slip to result in disaster for one or both of us. In the end, the only disaster was to this spanner as we shall see:


You get calcite growth on the threads of these caps which makes them quite stiff. We had spent a while belting the spanner with a hammer to get the nut to move, and you can see Keirhann is putting some effort into getting this cap off:


Here's the seat. It took me the best part of an hour to regrind it:


The other clack was worse. We hammered at the nut, or Keirhann did while I held the spanner in place, and eventually the end of the spanner moved. Unfortunately, the nut didn't:


This shows us why you use a proper forged flogging spanner when things are really tight - because cast tools will break. Fitter Bob welded it up again, and we took the propane torch to the clack body, which we probably should have done earlier as it came undone quite easily with a bit of heat on it.

Volunteer John was in today treating Wissington's wheels to some green undercoat:


For me, that was the end of the day. It was Friday afternoon, and all that remained was to tidy up and make sure we were ready for others to carry on after the weekend.

My next time on the railway will be a cleaning turn on Thursday 20th February - it is school half term week and we have a yellow service running (steam hauled train and a DMU, running four trips each). The B12 will be out - hopefully we will have some decent weather to show her off in her last year in service before her next overhaul.